Today we continued to work on different iterations of collector mechanisms. Our original prototype broke due to a standoff not being put on and we have since made changes to the design. The programming team continued to work on chassis code among others. Fabrication continued to work on milling out parts. The Chairman’s team made significant progress in cutting down our essay to the proper amount of characters. Electronics worked on making a pits checklist and troubleshooting design. Design worked on getting our electronics board ready.
Bear Metal Robotics