It was a successful day today we had lots of people show up. The programmers were busy programing and talking with a mentor on working to get the robot operational for the automatic mode in locating the crate and not something of a similar color that works with the camera in the crowd. Other events that happened today are one of the mills is stuck at a permanent zero because the wobbler broke so they can’t reset that mill.
That piece is ordered and we had to problem solve how to still face a part. Some can’t be worked on but some parts are still able to be done today. The rest of the milling is easy and there aren’t any problems on the mill.